Beobot 2.0/Electrical System/Prototype 1 CB
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| Revision as of 21:59, 3 Nov 2009 Siagian (Talk | contribs) ← Go to previous diff |
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| Line 4: | Line 4: | ||
| To Do | To Do | ||
| - | * Propeller sonar processing | + | * - |
| - | * Power connector (12, 5VCC) | + | |
| Done | Done | ||
| * Propeller USB connection | * Propeller USB connection | ||
| * Flowmeter reading processing | * Flowmeter reading processing | ||
| + | * Propeller sonar processing | ||
| + | * Power connector (12, 5VCC) | ||
| ==Cooling Board Results== | ==Cooling Board Results== | ||
| - | No catastrophic error yet. | + | No catastrophic errors. |
| ==Bug List== | ==Bug List== | ||
Revision as of 19:36, 6 Nov 2009
| Table of contents |
Cooling Board Objectives
To Do
- -
Done
- Propeller USB connection
- Flowmeter reading processing
- Propeller sonar processing
- Power connector (12, 5VCC)
Cooling Board Results
No catastrophic errors.
Bug List
- USB signal (D+ and D-) is flipped, we are fixing the problem by rewiring the legs of the USB B connector. We fixed the Altium file so that this is not needed in the future.
Logs
Thursday, May 7, 2009
Soldered the components unto the boards
Friday, May 22, 2009
USB connection is flipped because the Propeller USB (B+ & D-) definition is reversed
Friday, May 29, 2009
Wrote Frequency monitoring code for flowmeter. We blow on the tubes to simulate different flows.
Back to Electrical System
