Beobot 2.0/Electrical System/Prototype Final BackMainBoard
From ILabWiki
(Difference between revisions)
| Revision as of 19:31, 6 Nov 2009 Siagian (Talk | contribs) ← Go to previous diff |
Current revision Siagian (Talk | contribs) |
||
| Line 2: | Line 2: | ||
| [[Image:BackMainBoard Altium2D.JPG|390px]][[Image:BackMainBoard Altium3D.JPG|300px]] | [[Image:BackMainBoard Altium2D.JPG|390px]][[Image:BackMainBoard Altium3D.JPG|300px]] | ||
| - | Done | + | '''Done''': |
| * USB[0,1,2,3,4,5] out from each computer. There are a few that does not work. It's listed on the top of the main electrical section. | * USB[0,1,2,3,4,5] out from each computer. There are a few that does not work. It's listed on the top of the main electrical section. | ||
| * KVM power | * KVM power | ||
Current revision
| Table of contents |
[edit]
BackMain Prototype Final Objectives
Done:
- USB[0,1,2,3,4,5] out from each computer. There are a few that does not work. It's listed on the top of the main electrical section.
- KVM power
- KVM USB - propeller control
- KVM VGA - propeller control
[edit]
BackMain Prototype Final Results
No catastrophic error.
[edit]
Bug List
- USB hub board hits the USB8 adapter board. Fixed by placing it below the back main board
- USB common signal for D+ and D- is flipped. We twist the ribbon cable that goes into it. The permanent solution should be changing the library part of the hub.
[edit]
Logs
Thursday, May 7, 2009
Soldered the components unto the boards. USB hub has to be soldered below the board instead because of conflict.
Friday, May 8, 2009
USB Hub can use 100mil pitch (instead of the 2mm pitch)
Back to Electrical System
